Tuesday, October 03, 2006

Color of Money and Oil

I suppose that it's time to get you caught up with the car as opposed to my social life.

Its not good news. About the middle of September, I did put on the head for the Fourth time. I went through all of the manual steps, and used the advice of those who have done it before me. I got the car filled with oil, cooling fluids, etc. Took a bit of manipulation with regard to the distributor's static timing, but I got it to fire. During the idle period, I wanted to get excited, I wanted to hop around and feel proud of myself. But having been at this point before, I just decided to keep a level head and carefully evaluate the exhaust and monitor the oil.

In about 30 seconds I started to get wispy exhaust. The kind of exhaust that happens when there is excess moisture in the combustion chamber. Not good. So with heavy hands, I checked the oil via the dipstick. Sure enough I recognized the oil combining with water. Being that I don't regularly swear, I find it offensive, I'll type with some colorful characters. My words went something like this:

"F*k me to Tears!"

Got that one from dad years ago. I digress. I shut her down, closed the garage door and wanted nothing more to do with her that day.

About a week later, I started the disassebly, AGAIN! Gee, I think I hear the echo of my young daughter telling me, "Dada, again..."

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The color of money and oil

That is what it looked like when I took the cam box off the head. Without question you can see the green antifreeze mixing with the oil. Recall that the car had only idled for about a minute. It is weird that I got this amount of antifreeze in. I know that at this point your mind is whirling about the cause.

So to review, here is what was done in preparation for a successful rebuild.

Head was planed flat, and a valve job was completed.
Block surface was thoroughly cleaned and checked for flat.
A new FelPro Racing Gasket was used. (the gasket is the right one)
The torque process was followed to the letter.
Torque was stopped at 70 Ft/lbs.
The thermo housing opening was checked to insure that the EGR port was covered.
The head's manifold ports were checked to insure they were closed.

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Correctly designed FelPro


Now, here are my potential problems
The block was found to be .006 out of true between cylinders 2 and 3.
The head bolts could be generating a false torque.
I could have faulty Hex head plugs in the head.
The locating dowels could be too big.

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Hex head plugs could be an issue

Current status
The head was reinstalled with out the washers, I absolutely have outruled the head bolts creating a problem. The head is going to be pressure tested to insure that it is free of micro fissures or other unforeseen issues.

So, that is all the time I have for today. As I was telling the guys on XANA, thanks for not giving up on me.

Best,

E